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6.0L PowerStroke Engine & Drivetrain Discussion of subjects related to the 6.0L PowerStroke Engine & Drivetrain
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#1 |
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SDD Junior Member
Join Date: Jan 2012
Location: Centereach, NY
Posts: 8
Thanks: 1
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Greetings all; Ive spent 2 days surfing the forums to see if anyone else has these challenges.
#1. about 3 weeks ago the truck started to sputter and hesitate under load. Gray smoke filled the street like I had a smoke genereator installed on back. Then the turbo kicked in and the truck took off like a shot. Only happened once. Happened again today, worse though, now the check engine light is on. I scanned the code and received "actual turbo boost is less than expected turbo boost" no explanation. Parts store guys are scratching their heads. #2. Now my day time running lights wont illuminate nor will the automatic lights. Parking lights and running lights come on, but no headlights until you turn the knob. #3 the stereo cuts on and off. Was off for two days, Now its on again, but cant change any stations or raise or lower volume. #4 The power rear window no longer works. I dont know if these are seperate issues or all related to some electrical short. I had an electrical guroo here for 3 hours and he could not find anything on the scanner or any loose or bad connections under the dash. He also checked every fuse and everyone of them is good. Any suggestions??? Im a carpenter. Im handy with a wrench if I know what Im looking for. Thanks |
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#2 |
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SDD Junior Member
Join Date: Jan 2012
Location: Centereach, NY
Posts: 8
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Ive already cleaned the EGR, installed new orings, cleaned the passage ways around the EGR, changed the MAP Sensor, New hose to the map sensor from manifold, ANd cleaned the Waste Gate Actuator on the turbo. THE EGR moves freely with only hand strength. the Waste Gate moves freely when pressing on it.
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#3 |
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SDD Senior Member
Join Date: May 2005
Location: Ukiah, California
Posts: 7,866
Thanks: 127
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There is no wastegate on a 6.0. It is a variable vane design that changes the pitch as you need more boost. You must have moved the actuator for the vanes.
Dave
__________________
2004 F-350 Regular cab with 6.0, Torqshift, 4X4, and just about all of the rest of the options. I added Guages, Satellite Radio, Air Horns, and a coolant filter. Bilstein shocks. Battery Desulphater that really works. Installed Jimmi Jammers. Pictures here: http://community.webshots.com/user/dbennett48 Completely Stock. I had a Detroit Diesel 8V92TA in a KW dump truck in 1980. That sucker would put out 425 hp but would never out pull a CAT. |
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#4 |
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Dogman
Join Date: Nov 2007
Location: tampa,FL
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Check your batteries and there cables. Have them load tested the batt.s one at a time first. These trucks are really picky about there voltage. Sounds like a bad ground from the batt.s.
__________________
2008 F-250 All stock so far...LOL 1999 Jeep TJ play toy on 32" tires custom bumpers by me
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#5 |
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SDD Member
Join Date: Jun 2009
Location: Mississippi State
Posts: 341
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Thanked 27 Times in 26 Posts
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Like Dogman says, electrical connections are bad. This engine has to have proper voltage or they will not function properly. Take both batteries out and have them tested individually. Clean all cables and battery post if the batteries check out ok. Reconnect them. If batteries re bad or even if one is bad, buy a new matched pair of batteries. Make sure all the connections including ground to frame connections are clean, tight and good.
__________________
![]() 2004 F250 Crew Cab King Ranch Lariat FX4 Saddle Leather 6.0 L FUMOTO Valve AIRAID 4" straight No CAT No MUFF Nitto Terra Grapplers All Terrain LT285/75R16 10 PR Everything else pretty much stock NEW Ranchos installed 8/15/2010 Anyone Got Birds? Will Travel to Hunt!We are all just Village Idiots,
Enamoured with our own shadow, Oblivious to the setting sun! |
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#6 |
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SDD Junior Member
Join Date: Jan 2012
Location: Centereach, NY
Posts: 8
Thanks: 1
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Smokey, Dogman, will do that next. This am (0500) radio was working, power windows did not work, daytime running lights were working. This is gonna be fun isnt it.
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#7 |
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redneck punk
Join Date: Aug 2008
Location: idaho
Posts: 75
Thanks: 1
Thanked 4 Times in 4 Posts
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ive seen this kind of electrical issues before on the gassers mainly but water getting on the fuse block thats under the dash from water leaking in the front windsheild getting on it and causeing alot of electrical issues
just another thing to check
__________________
97 f 250 crew cab, 3 in down pipe 4 in back exhaust, afe intake, built trans, diy intercooler and pipes regulated return fuel system, water meth, stg one injectors. 6 pos chip tuned by tyrant |
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#8 |
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SDD Senior Member
Join Date: May 2005
Location: Ukiah, California
Posts: 7,866
Thanks: 127
Thanked 505 Times in 488 Posts
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This will cause problems in the diesel trucks also. The water runs down onto the fuse block and the resulting corrosion plays havoc with the truck.
Dave
__________________
2004 F-350 Regular cab with 6.0, Torqshift, 4X4, and just about all of the rest of the options. I added Guages, Satellite Radio, Air Horns, and a coolant filter. Bilstein shocks. Battery Desulphater that really works. Installed Jimmi Jammers. Pictures here: http://community.webshots.com/user/dbennett48 Completely Stock. I had a Detroit Diesel 8V92TA in a KW dump truck in 1980. That sucker would put out 425 hp but would never out pull a CAT. |
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#9 |
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SDD Junior Member
Join Date: Jan 2012
Location: Centereach, NY
Posts: 8
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Thanks again gentleman, Ill pull the fuse block out its only held in with 4 bolts. I did find that I have a remote start and an alarm ALREADY installed in teh truck. Im going to start with someone looking at the remote system, Im thinking this may be the root of my issues. It doesnt look like it was installed so well.
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#10 |
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redneck punk
Join Date: Aug 2008
Location: idaho
Posts: 75
Thanks: 1
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alarm system cause more problems than they do good, just my opinion
__________________
97 f 250 crew cab, 3 in down pipe 4 in back exhaust, afe intake, built trans, diy intercooler and pipes regulated return fuel system, water meth, stg one injectors. 6 pos chip tuned by tyrant |
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