iracemine
black and tan
WOW, not looking forward to this. is this somthing thats just a maintenance thing or mainly for moders???
Alright here goes for all those that have been awaiting a reply.
I did it took the plunge and did it. I pulled the turbo off the truck, this was a piece of cake to do. I had the turbo and pedestal off in about an hour maybe a little less. Then came the hard part of the whole damn thing. I couldn't get the bolts out of the baby butt connector. I was gonna try and do it with out removing the up-pipes from the manifold.
I ended up having to take the up-pipe off the passenger side manifold. Then I was able to remove the whole baby butt connector. After that the bolt came out easily.
I did as others have suggested and slathered everything in anti-seize. Then I started putting stuff back together I thought I left everything loose enough but I didn't and it became a royal PIA to get the baby butt connector to match up to the turbo again. Leave everything loose when putting back together.
I still have a problem though, the drivers side has not sealed up properly, so it still leaks. I have to figure out away to try and get it sealed up. Just need another couple of free hours.
Get yourself a 10mm universal socket and at least 36" of extension and you will be in good shape. A 10mm ratcheting wrench will come in handy also. Those would really be the only important things to have.
If you have any other questions let me know. I was kinda vague and will right edit some details when I get the chance.
WOW, not looking forward to this. is this somthing thats just a maintenance thing or mainly for moders???
Hey Kent when you round off the bolts in the baby butt, which I am guessing you will do to at least one of them. I know I did. Then drive a 6 point 3/8's socket on there and remove the bolts that way.
I haven't gotten around to fixin my drivers side leak. Gonna do that next weekend.
Let us know if you experience any difference in boost. I believe I gained about 3 lbs, which puts me to 30psi.
the SES light came on cause of overboost.